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PanzerJohn

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Posts posted by PanzerJohn

  1. Keith

     

    I had an identical situation with a pannier and , like you, I was able to fix it because all the gear wheels were accessible.

     

    I may be mistaken but I wasnt able to strip the Dean down that far

     

     

    My first Dean, a reliveried BR version, runs very well but I fitted it with a surplus TCS stay alive chip......I dont know whether the capacitor power is sufficient to overcome the hesitation at that one point in the cycle? The second Dean hesitates and then stalls at slow speeds.

     

    John

    The second Dean hesitates and then stalls at slow speeds.

     

    That's what mine was doing.

  2. My 3rd replacement Dean has now started stalling at low speed and refusing to restart unless given a large and abruptly applied dose of power. It's going back to Oxford this time.

     

    Got it back with a new chassis/motor fitted, performance as it should be now, still gives most of its performance range with a very small amount of control knob turning so I have to be quite delicate with power control from the start or it takes off like a dragster but I've got a Bachmann City of Truro like that too.

  3. I've had nothing but trouble with twin flywheel version, on my third now and it's started stalling at low speed. I won't be buying any more Oxford tat, it's a shame as it's such a well detailed and good looking loco.

  4.  

    Having done some more research I can say the missing bit of pipework along the RH footplate edge (Hanging plate) is not missing at all. That pipe is the ATC conduit which, at the point it stops, should go through the footplate and up the front of the cab into the control gear in the cab, 

     

    Unfortunately Oxford Rail has missed a bit of pipe out but not the bit along the edge of the footplate.  I understand that locos were only fitted with ATC after 1930/1 so any loco intended to be prior to that date needs the pipework removed entirely. This would include 2309 and the WW1 variant of course. 

     

    Hope the information is of some help to someone in case they think their loco is missing some ATC conduit.

     

     

    The weird thing is that one of the locos had complete pipework on BOTH sides!, I wonder if they have a little man at the factory with a Stanley knife cutting them down and he got that one wrong!

  5. Further to the above.

     

    Decoder is totally fried.

    I replaced it with a blanking plug and tested the loco on DC on a bench power supply.

    It shows that as the wheels rotate there is a complete short at certain points in the rotation. A bit of a strange fault

     

    It'll have to go back whence it came.

     

    Keith

     

    Your problem may be the prob Oxford told me ref my previous post.

  6. I had to send 3 back before I got one that runs reasonably, all 4 have had missing detail parts, the tiny hook by the the front left buffer (2),missing the rear half of the pipework that runs alongside the running board (3), l/h brake rod (1), fallen out tender buffer (1). 2 were particularly poor runners, I phoned Oxford and was told they had probs with some the early ones which was down to shorting on the chassis halves, now cured by painting the previously bare metal surfaces. I have to say that imo they are not particularly sprightly runners compared to say, a Hornby Q1. It seems to run out of puff at half power on my controller but reaches a reasonable speed pulling 3 Hornby Mk1'sl, the speed range is basically covered by a quarter turn on the controller, the remaining 3 quarters give no more rpm from the motor. I was tempted to return it but it's such a nice looking well detailed model and was only £80 that I'll keep it, but am a bit wary of any future Oxford purchases.

  7. I've picked up 2, one Hornby wishy washy green and one in lovely blue, both under £80 (new). Great value, I'm a sucker for detailed cabs and these are the bees knees.

    • Like 1
  8. Mine has a click too, can't seem to find out where it comes from. I'm going to refer to this as a "slider bar" and the lower part or it popped out. I eased it back into place and gave the loco a quick lubricating wherever the instructions said so. It runs brilliantly. The clicking has reduced drastically and only turns up some times but nowhere near as loud as it was .

    Check that the piston con rod isn't catching the nut on the front driving wheel on bends when the wheel is at it's most lateral movement. Sometimes you need to bend the rod out a little to clear the nut.

  9. Got my Warley special today and yes it has " the problem".It will pull 3 staniers but takes only the lightest touch from the hand of god to stop it dead, and it wheelspins really easily on abrupt power application. Shame as it's a really nice model for the money. Solutions are, from Hornby slightly thicker traction tyres or myself is to file a couple of thou off the rear axle slot. I wil ltry and get hold of some Airfix or Dapol traction to see if they are any thicker than the current Hornby ones.

  10. I examined one at a Toy Fair a couple of weeks,spotted a small nick/gouge on the left cylinder.Dealer not happy, although he said he'd get a refund from Hornby on returning it there were none left to replace it so he'd loose the profit on the sale. He said it was a fairly common thing with Hornby these days.

  11. Just been looking at some of the new Warley vids on YouTube, and the 14xx seems pointedly absent from H's trade stand...

    A mate picked me up the Show Special one there yesterday. Can't wait to get my hands on it, looks really nice.

  12. My bargain S15 arrived within 24 hours of ordering from deepest Cornwall and is a beautiful bit of kit.I gave it a good checkover first and nothing was loose and it is proving to be a beautiful runner. The cab detailing is exquisite, at £80 you can't beat it.

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