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Ian Morgan

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Everything posted by Ian Morgan

  1. June 2007: I was unhappy with the worm gearbox. With just the motor and worm fitted (no gears) it was very rough compared to when the motor was out of the gearbox. Flexing the gearbox did allow the motor to speed up, but I just could not make it stay like that. Eventually I realised the gearbox had folded up not square. I removed the bearing from the far end and the worm rod was naturally hard against the side of the mounting hole rather than in the middle. I took the gearbox apart at the fold lines, filed the edges square and soldered it back together square, so that the worm rod was central to the bearing mounting hole, and when the bearing was added, the motor still ran smoothly and very, very slowly. Now I think I stand a chance of making it work with some gears in position too. However, I want to blacken the chassis first. June 2008: It is over a year since my last posting. I had been making excuses, such as pressure of work commitments, life, looking for a good way of blackening the chassis, etc, but mostly it was down to being disappointed in how the chassis was running. Anyway, Friday 6th June, I got all the bits out of the box again. The rusting tube the worm is mounted on was cleaned up with emery and oiled, and found to be running smoothly in the chassis with just the worm gear on its idler shaft. Adding the next idler gear messed things up though. It looks like the worm gear is slightly non-concentric on its shaft. The bearings have been opened up to give a little play, but adding the next gear took away thay play. So, some more careful opening up of the bearings eventually resulted in free running of the gears. By now, the stub axles used by the idler shaft muffs were quite a loose fit, and kept dropping out. It was time to glue them in place. For the second shaft, with the breather hole drilled in it, this was a simple matter of applying some super glue into the hole on the end of a pin. The worm gear shaft is trickier, because there is no room for such a hole. I inserted a small piece of plastic rod to ensure the two stub axles can never meet in the middle. Then I tried adding some glue into the ######, putting it into position, then inserting the stub axles through the bearings. First I tried superglue, then I tried Uhu. No real success with either, except that I managed not to glue the ###### to the chassis. However, the stub axles are now a tighter fit, and might stay put. The rear wheels were fitted next. The ###### had to be reamed out quite a lot, but still retaining a tight grip on the half axles. Everything was still nice and smooth. Adding the centre wheels locked the whole chassis up though. The gear was hitting the solder and folded tab of the spacer fitted above it. The solder, and some of the tab was carefully filed/chiselled away until there was clearance. The same was done for the front wheels, but eventually, on Friday 13th, all wheels were turning sweetly, and very slowly, under motor power. The chassis had been blackened using a CD marker pen. It needs touching up after all the fettling, but it is a quick, easy way to do it.
  2. 3 Feb 2007: Last night's session started by me having to free up the rusting worm tube and extract it from the bearing. I cleaned it up again with emery paper, and got everything running freely again, but left it dismantled this time. I must put some oil on it to stop it rusting again. Having dismantled everything, this evening was a less-than-exciting session of drilling .35mm holes (the smallest surviving drill I could find in my toolbox). Twelve holes in the chassis, and another 18 in the folded up brakes. However, I managed to complete all this without breaking a drill, which makes a nice change for me. I then cut 18 half inch lengths of .3mm nickel-silver rod ready for soldering,but as I did not have any balsa wood, that will wait for the next session. Part 2 This Friday I had balsa wood (courtesy of Dave Stratton) so I could add the wires cut during the last session to the brakes. At this point we noticed that there are another set of brakes on the thinner etch. I presume these would have been easier to fold and drill than the ones on the thick etch, but maybe not so strong in use, so we will use the thicker ones. Threading in the wires, and soldering up, as per the instructions,was straight forward enough, and the photo shows them with most of the wires trimmed and cleaned up. I will cut the remainder later, as I expect the length will be critical to hold them in place with the outer frames, without fouling the gear chain on the one side. The next stage will be to paint or blacken the frames and wheels ready for final assembly before progressing with adding the cranks and connecting rods.
  3. Yes, I will add the Freshwater blog once I have caught up with things, then I have some new stuff to add as work on Freshwater is progressing.
  4. Thanks for the kind words about my soldering, but rest assured, it ends up not so neat later as I make adjustments and changes.
  5. 20 Jan 2007: I started by cutting up bits of the axle steel into bits approximately 3.5mm long, using a vice and slitting disk. The gear muffs were drilled and reamed until the axle steel would push into them (1.6mm drill was used eventually). I fitted the lay shaft with the gear at each end first, using a 1.5mm drill first, then pushing it through with one of the short lengths of axle steel. This method worked quite well. The larger gear was catching on the stretcher tab, so it was filed back a little to clear the gear. Next would be the worm gear lay shaft. The merf for this one needed shortening as the bearings are further in (Note that the automatic censor on this blog does not like the singlular form of muffs, so i will have to call them merfs from now on). Another problem is the fitting of the gearbox over one of the bearings. Excess solder was filed away to allow it to fit, but it was apparent that one of the gears on the already fitted lay shaft needed to be away from the end of the merf to clear the gearbox. The smaller gear had been glued to the end of the merflast week, but the larger gear could be pushed right up to the collar to give clearance. It does mean that the gear train to the wheels is on the opposite side to the model in the instructions, but hopefully that will not cause more problems. To turn that lay shaft round, I had to file the other stretcher tab to clear the larger gear. You can see the gearbox tab and how it fits next to the gears in the bottom left of the second photo. Note that the tube that has the worm on it is rusting rapidly, although I am sure I did not get any flux near it. With the two lay shafts and the gearbox in place, power was applied, and it whirred away smoothly, but slowly. Very satisfying, but I think it needs loosening up a bit. Not sure yet if the gearbox has to be fixed in place, or left to float.
  6. 13th Jan 2009: Last night's session was to be remembered for the things I forgot, like my glasses, and soldering iron. First of all, I corrected the previous week's mistakes, as pointed out on the VAG. The errant frame spacer was repositioned to the top of the frames, and Dave Stratten let me have a spare motor bearing so that I could complete the gear box. Getting the worm onto the tube was tricky, but do-able. However, it seemed to close up the tube so that the motor not longer fitted into it. I therefore pushed the worm down towards the other end of the tube which the motor still fitted. Having soldered the bearing in place, I could not fit the motor to the gearbox. Dave could fit his, but the motor would not turn when volts were applied. I therefore, unsoldered the bearing, assembled the gearbox, and then fixed the bearing where it wanted to be with a quick touch of the soldering iron. Dave did the same, and both motors whirred away happily. Next came sorting out which gears go where. Hopefully the photo shows the correct arangement. I drill the muffs in the centre with a 1.6mm drill to aid in applying glue, and allowing air to escape. One of these holes can be seen in the photo. Most gears were a good tight push fit, but two of the small gears were rather loose. I filed a flat on the black plastic, and a key into the inside of the gear, and applied araldite (see the lower left gear in the photo). I also put some araldite into the worm tube and fitted it to the motor. Thankfully the motor still turns today. The next stage is fitting stub axles, but as nobody had remembered to bring a minidrill to cut the axle steel, that will have to wait for the next session.
  7. I started chronicling the construction of my 09 on another blog elsewhere, but it did not seem to get much readership, so I have now started moving it across to rmweb where it might be of use/interest to more people. 5th Jan 2007. Was it really that long ago I started building my 2mm Scale Association 08 kit? This is what I wrote then: After checking the box contents, and the contents of the CD on a laptop, construction started.The instructions are clear and well illustrated, but definitely not for the novice, as has been stated. It starts off with the jig: here it is on the etch, here is a photo of the completed item, get on and build it. Fair enough, no problems there. Next the bearings were soldered to the frames, fully populated for all axles gear driven, using the thought that it will be easier to leave out idler gears later than to add more bearings. Now it was time to solder in the frame spacers. The quantity and positions seem to be at the whim of the constructor. The instructions state that various ones are optional, but does not indicate which ones, or why. The photos seem to be of two different sets of frames with different spacer populations. I eventually opted to put in 6 spacers. I remembered an earlier post on the 2mm VAG, so I made sure all the tabs were as close as possible to 90 degrees. The PCB strip was a lttle wide, so needed a little filing to fit. Also, my nice neat insulation gaps were too far apart, and had to be widened for some of the longer tabs.Trial fitting the gears will have to wait until next week, as the steel axle rod will need cutting up with a slitting disk. Therefore, I proceeded to put together the gearbox. Hmmm. The gearbox needs another bearing, but all the bearings supplied with the kit have been used up on the frames. Another job that will have to wait until next week. Anyway, the results of my first session can be seen below, cruelly magnifying my untidy soldering, showing the jig on the left, the gearbox at centre, and the chassis to the right.
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